burnthebox Posted January 30, 2013 Posted January 30, 2013 HI ALL, WHERE DID I READ ABOUT A RUNAWAY CRASH INTO BUFFERS, THANKS IN ADVANCE Quote
0 Garfield Posted January 30, 2013 Posted January 30, 2013 Where and when is it supposed to have happened? Quote
0 burnthebox Posted January 30, 2013 Author Posted January 30, 2013 Hi Gar, I think it was about 10, 15yrs. ago, & it was a 141 I think, Quote
0 ttc0169 Posted January 30, 2013 Posted January 30, 2013 Hi Gar' date=' I think it was about 10, 15yrs. ago, & it was a 141 I think,[/quote'] Hi burnthebox, It must be loco 191 that you are referring to, 15th August 1991-Northwall to Clonsilla, See more info about this in my layout Tara Jctn thread as I have a model of the withdrawn 191 on it and hgricer put up some details of what happened. Quote
0 irishthump Posted January 30, 2013 Posted January 30, 2013 Hi Gar, I think it was about 10, 15yrs. ago, & it was a 141 I think, 191 went AWOL at the North Wall in '91. (Something poetic about the way that sounds!) Crashed into some buffers and caught fire I believe. Quote
0 Broithe Posted January 30, 2013 Posted January 30, 2013 Hi burnthebox,It must be loco 191 that you are referring to, 15th August 1991-Northwall to Clonsilla, See more info about this in my layout Tara Jctn thread as I have a model of the withdrawn 191 on it and hgricer put up some details of what happened. From here on - http://irishrailwaymodeller.com/showthread.php/67-Tara-Junction?p=8305&viewfull=1#post8305 ... Quote
0 enniscorthyman Posted January 30, 2013 Posted January 30, 2013 She was the first GM to be scrapped.There was fire damage around the fuel tank and mid section.She was at the back of Inchicore works for a few years,grounded with no bogies and stripped of all useable parts.Very sad sight to see,and at one stage IE were going to rebuild this loco and a number of locos such as 161,132,174,126,and the long stored 125 and return to service,but the large influx of railcars put paid to that.actually 121 herself was also one of these locos as she was damaged on the weed killer train fire in New Ross in 1995. Quote
0 burnthebox Posted January 30, 2013 Author Posted January 30, 2013 191 went AWOL at the North Wall in '91. (Something poetic about the way that sounds!) Crashed into some buffers and caught fire I believe. Hi all & many thanks, yes there's definitely something poetic about that number, 191 in 1991, now better get back to work, Quote
0 krose Posted January 30, 2013 Posted January 30, 2013 Great pics of the remodelled scene, ttc Quote
0 ttc0169 Posted January 30, 2013 Posted January 30, 2013 Great pics of the remodelled scene' date=' ttc[/quote'] Thanks krose,something different. Quote
0 burnthebox Posted January 30, 2013 Author Posted January 30, 2013 Many thanks lads, & ttc what a layout, I just love the detail, to say I'm envious is just a hope that one day I'll have something like it, keep the story lines coming, bloody fantastict, ( PS ttc I got so carried away looking at your layout I nearly put this reply into your Tara Jcnt layout, what do's that tell you, ) Quote
0 snapper Posted January 30, 2013 Posted January 30, 2013 082 Ran away and it the buffers in Portlaoise loop on 29th of September 2011 Quote
0 h gricer Posted January 30, 2013 Posted January 30, 2013 More information on the 191 Clonsilla incident in this thread http://irishrailwaymodeller.com/showthread.php/67-Tara-Junction?p=8903#post8903, if I got a euro for everytime I retolded it, Id be a millionaire now. Regards h.gricer Quote
0 josefstadt Posted January 31, 2013 Posted January 31, 2013 Don't forget the incident at Cobh on 5 May 1995. Locomotive 165, working an early morning empty passenger train, failed to stop at the station's platform, crashed through the buffer stop, ploughed through the wall of the Cobh Heritage Centre and ended up partly inside the centre's exhibition hall. Quote
0 heirflick Posted January 31, 2013 Posted January 31, 2013 082 ran away and it the buffers in portlaoise loop on 29th of september 2011 any more info on this snapper? Quote
0 heirflick Posted January 31, 2013 Posted January 31, 2013 She was the first GM to be scrapped.There was fire damagearound the fuel tank and mid section.She was at the back of Inchicore works for a few years,grounded with no bogies and stripped of all useable parts.Very sad sight to see. indeed she was a sorry sight, found a pic of her........ Quote
0 snapper Posted January 31, 2013 Posted January 31, 2013 any more info on this snapper? A full report into the incident is available here (Link) Quote
0 Broithe Posted January 31, 2013 Posted January 31, 2013 A full report into the incident is available here (Link) Very interesting. I see that it shoved the buffer stop nine meters and left it undamaged - as we discussed friction buffer stops recently - http://irishrailwaymodeller.com/showthread.php/1418-Irish-Bufferstops?p=20861&viewfull=1#post20861 Quote
0 heirflick Posted January 31, 2013 Posted January 31, 2013 A full report into the incident is available here (Link) fair play to you Snapper - thanks for that! poor old 082.......i wouldnt mind but on my days off im usually down there at that concrete buffer takeing pics of anything that moves - some fright to get seeing her comming down at you!!! worse still, emagine if she was powering up and hit the buffer at speed, derailed and hit the wall - some drop there! Quote
0 Broithe Posted January 31, 2013 Posted January 31, 2013 fair play to you Snapper - thanks for that! poor old 082.......i wouldnt mind but on my days off im usually down there at that concrete buffer takeing pics of anything that moves - some fright to get seeing her comming down at you!!! worse still, emagine if she was powering up and hit the buffer at speed, derailed and hit the wall - some drop there! And double yellows, too - they would get some fair ticket for parking it there... Quote
0 heirflick Posted January 31, 2013 Posted January 31, 2013 And double yellows, too - they would get some fair ticket for parking it there... Quote
0 h gricer Posted January 31, 2013 Posted January 31, 2013 (edited) Don't forget the incident at Cobh on 5 May 1995. Locomotive 165, working an early morning empty passenger train, failed to stop at the station's platform, crashed through the buffer stop, ploughed through the wall of the Cobh Heritage Centre and ended up partly inside the centre's exhibition hall. I had forgotten about that, there have been a few in resent years, 21st July 1994 locomotive 073 derailed on the trap points at Newcommen Junction with a Sligo liner, it very nearly ended up in the Royal Canal. On the morning of Wednesday 9th April 2003 201class locomotive 215 was involved in a very spectacular derailment at Heuston while shunting the MK2 AB coaches, the incident happen early in the morning, by 11am 215 was leaning at a 45degree angle in danger of topping over, ballast was put under the loco to support it, then 2 road cranes had to be brought in to ''stabilize the loco'' press photographers where hunted off the site, but the photos still appeared in newspapers the following day. Regards h.gricer Edited February 13, 2013 by h gricer Quote
0 heirflick Posted January 31, 2013 Posted January 31, 2013 On the morning of Wednesday 9th April 2003 201class locomotive 215 was involved in a very spectacular derailment at Heuston while shunting the MK3 Int coaches, the incident happen early in the morning, by 11am 215 was leaning at a 45degree angle in danger of topping over, ballast was put under the loco to support it, then 2 road cranes had to be brought in to ''stabilize the loco'' press photographers where hunted off the site, but the photos still appeared in newspapers the following day.Regards h.gricer now thats a pic i would love to see! Quote
0 josefstadt Posted February 2, 2013 Posted February 2, 2013 On the morning of Wednesday 9th April 2003 201class locomotive 215 was involved in a very spectacular derailment at Heuston while shunting the MK3 Int coaches, ...Regards h.gricer And, no doubt someone high up in the company thought 'must get rid of the MkIII stock to prevent this happening again'!!!!! Quote
0 enniscorthyman Posted February 2, 2013 Posted February 2, 2013 075 was a unlucky loco with the Buttavant crash in 1980, and she ran into the back of a liner and ended up on her side sometime in the 90s. Quote
0 Railer Posted February 4, 2013 Posted February 4, 2013 Amazing the amount of people around the crash site with the cranes on scene. The days before health and safety. Quote
0 Railer Posted February 4, 2013 Posted February 4, 2013 Back in the days when the wash road at Connolly yard was a good bit shorter than it is now. Quote
0 heirflick Posted February 4, 2013 Posted February 4, 2013 excelent pics railer! was 171 a right off or did she survive? Quote
0 Warbonnet Posted February 4, 2013 Posted February 4, 2013 excelent pics railer! was 171 a right off or did she survive? She lived to fight another day Seamus Would never be rebuilt now. Quote
0 heirflick Posted February 4, 2013 Posted February 4, 2013 id love to see the p/way gang recover her! Quote
0 Railer Posted February 4, 2013 Posted February 4, 2013 Funny enough 171 was the last baby GM in service. Spent it's last days shunting between Pearse, Connolly, North Wall and Heuston. Quote
0 heirflick Posted February 4, 2013 Posted February 4, 2013 Railer, any more pics of railway accidents ? Quote
0 h gricer Posted February 4, 2013 Posted February 4, 2013 And, no doubt someone high up in the company thought 'must get rid of the MkIII stock to prevent this happening again'!!!!! My mistake josefstadt, it was actually the MK2 (ABs) stock that 215 was shunting when it derailed, that stock used to work the 10.00 Heuston / Limerick, found the slide which I must scan. Regards h.gricer PS hard to believe 171 survived another 35years after the wash road incident. Quote
0 Railer Posted February 4, 2013 Posted February 4, 2013 Railer, any more pics of railway accidents ? They are just a few I have sitting on a hard drive. I one or two of an A class runaway accident in Cork freight yard and another of a 121 on a Mk3 PP working, derailed on the Northern Commuter line. Also a bad scanned picture of 225 after it's fatal level crossing accident 2 years ago, it's still not repaired and most likely never will be. Quote
0 Railer Posted February 4, 2013 Posted February 4, 2013 I've no back story to this event at all of how or what exactly happened. Quote
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burnthebox
HI ALL, WHERE DID I READ ABOUT A RUNAWAY CRASH INTO BUFFERS, THANKS IN ADVANCE
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